You can set the sort order of messages? Just click on the link in the date column. Your preferences will be remembered, so you don't have to do it again when you return.
Welwyn , that's it, I couldn't remember last night (I'd just got in from a hairy day followed by a 200 mile drive!)
I've got a big tin of Welwyn resistors but they're buried under a great pile of junk (my wife's word!) in the garage but many thanks for the offer Graham. I do have an RS 7W item to hand though so I'll fit it later today,
Cheers,
Jim
From: Graham Adcock <adcock@...> To:
eddystone_radio_users@... Sent: Thursday, 14 June 2012, 23:53 Subject: Re: [eddystone_radio_users] Re: 680X query

As you say Jim, similar to Zeners.
The green resistors are probably Welwyn - vitreous. Good bits of kit in my opinion. Probably got one if you're stuck...
Cheers Graham. I only placed this query initially because the original resistor looks like a 12W item - one of those green glossy vitreous W...... types,
73,
Jim
From: Graham Adcock <adcock@...> To:eddystone_radio_users@... Sent: Thursday, 14 June 2012, 23:42 Subject: Re: [eddystone_radio_users] Re: 680X query

Jim - the 4.5W you've calculated is correct for a 300V HT (300 - 150) x 30mA = 4.5W. This runs the 150V regulator at its maximum current.
However, the 20mA taken by the 2 valves connected to the stabilised supply will come out of that maximum current, reducing the regulator current by 20mA to 10mA but maintaining the 30mA through the dropper resistor and maintaining 4.5W.
At a guess, the original 2k7 indicates a supply nearer 250V. In any case, the 4.5W will be fine in a 7W resistor.
Many thanks for getting back to me - so that should give 4.5W (assuming 300V HT). I think the 2 valves obtaining their HT from the VR150 take about 10mA each though which gives another 3W so 7.5W absolute maximum. I think I'll get away with it then! (At least until I find a 12W resistor!)
Best wishes,
Jim
From: "rkavampsev@..." <rkavampsev@...> To: eddystone_radio_users@... Sent: Thursday, 14 June 2012, 9:43 Subject: [eddystone_radio_users] Re: 680X query
Hi JIm
Measure the set ht and you know the vr150/30 draws 30 milliamp max at 150 v so set ht, minus 150 v times 30 milliamp equals wattage of dropping resistor
I've connected up the new resistor and it's drawing 47mA which makes just under 6W dissipation. I was surprised at how hot it runs though (having burnt my finger on it). 6W doesn't sound much but it's a tenth of a table lamp's 60W bulb dissipation after all. I'll fit a replacement 12W item when I unearth my tin! I've had spinal surgery recently and am banned from rummaging in the tip.i.e.garage by SWMBO!Thanks everyone,
Is 47mA not a bit high, considering 40mA is the absolute max for the VR150? I know that less than this actually flows through it under normal conditions but under fault conditions it could receive the whole lot. I'm surprised that Eddystone didn't make R66 higher which they could easily have done and still had enough current for the HF oscillator, BFO and mixer anode. I had a sudden thought that the previous owner might have had the mains transformer set to 200V accidentally but that isn't the case. Still the HT Voltage does seem a bit high at 275V.
I found a stray wire in the BFO compartment which had come undone from the earth tag on the BFO transformer. At first glance it seems to be earthing some front panel controls, but these are already earthed elsewhere. Anyway I've reconnected it and it
doesn't make any difference to the working. A bit of redundancy, I suppose.
One thing, there's nothing like a bit of fault finding to help you get to know your set!
Jim
From: Jim Jobe <jimjobe1@...> To: "eddystone_radio_users@..." <eddystone_radio_users@...> Sent: Friday, 15 June 2012, 14:03 Subject: Re: [eddystone_radio_users] Re: 680X query
I've connected up the new resistor and it's drawing 47mA which makes just under 6W dissipation. I was surprised at how hot it runs though (having burnt my finger on it). 6W doesn't sound much but it's a tenth of a table lamp's 60W bulb dissipation after all. I'll fit a replacement 12W item when I unearth my tin! I've had spinal surgery recently and am banned from rummaging in the tip.i.e.garage by SWMBO!Thanks everyone,
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
Best wishes,
Jim
From: "rkavampsev@..." <rkavampsev@...> To: eddystone_radio_users@... Sent: Friday, 15 June 2012, 14:13 Subject: Re: [eddystone_radio_users] Re: 680X query
Hi Jim
Something wrong here
If its drawing 47 ma then the stabaliser valve isnt within its working capacity
Pull out the two valves that the stabaliser is for and see what the vr150/30 draws itself .
i suspect you have a faulty cct about one of the valves that the VR150 is designed to stabalised .
The plot thickens! I've just measured the HT voltage again (DMM) and, with the Archers tuned in on R4 MW, I'm getting 300V at the rectifier side of the choke and 283V on the other side of it. The 265V quoted by Eddystone in the handbook is for the rectifier side and isn't, as I thought, the main HT line voltage which should be about 220V with a 1000 ohm/Volt meter.
This means that the transformer output is way too high by 60-70V. It seems to be the original Eddystone component and the input is set to the 230V position so I'm totally at a loss now as to why this should be so high.
Any suggestions gratefully received! This set seems to have the same jinx as my computer - it develops faults that no-one else has ever heard of! I only bought the set last year and haven't used it
much. but I've long suspected its performance isn't up to scratch.
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim Jobe Sent: June-15-12 8:55 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
I take on board all you've said. That's a useful tip on how to simulate a low impedance meter and I'll try that for comparison purposes. I've been using a DMM and also an AVO8 (see above for latest measurements as compared with another chap's set). When all's said and done though there is still that high current (47mA) through R66, measured with a series milliammeter, which is what alerted me in the first place and probably caused the original R66 to burn out, as well as, possibly, C115. I'll keep everyone in touch with what develops,
best wishes,
Jim
Quote:
Originally Posted by g4aaw pete
As promised, measured on Fluke 87
a/c input = 244v a/c
a/c o/p from transformer from ' 0' terminal to ' 250 ' terminal = 271v a/c
Chassis to rectifier side of choke = 262v d.c.
Other side of choke = 249v d.c.
Hope that's useful.
Regards
Pete
Cheers Pete,
My measurements for transformer using AVO8:
i/p: 244VAC
o/p: 266VAC
6.3V 3A winding: 6.6VAC
Chassis to rectifier side of choke: 300VDC
Other side of choke: 283VDC
So, my output to the rectifier is actually lower than yours Pete, yet the final DC HT is considerably higher. What on earth is happening?
Jim
I've just had a thought: there's another 40uF capacitor wired across the
original by a previous owner. I've assumed this is because the original
is duff but what would happen if it wasn't? I would then have the equivalent of an 80uF smoothing capacitor - would this cause a rise in HT voltage?
Last edited by jim_jobe; Today at 01:51 PM.
From: Gerry O'Hara <gerryohara@...> To: eddystone_radio_users@... Sent: Saturday, 16 June 2012, 15:55 Subject: RE: [eddystone_radio_users] Re: 680X query
Hi Jim,
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in
the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate
to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim Jobe Sent: June-15-12 8:55 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5%
in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
Yes, there is still that original issue and as I think Roy noted, most likely a component problem on the circuits supplied by the stabilizer (have you tried changing the stabilizer by the way? – perhaps it is faulty).
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim Jobe Sent: June-16-12 8:44 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query
Hi Gerry,
I take on board all you've said. That's a useful tip on how to simulate a low impedance meter and I'll try that for comparison purposes. I've been using a DMM and also an AVO8 (see above for latest measurements as compared with another chap's set). When all's said and done though there is still that high current (47mA) through R66, measured with a series milliammeter, which is what alerted me in the first place and probably caused the original R66 to burn out, as well as, possibly, C115. I'll keep everyone in touch with what develops,
best wishes,
Jim
Quote:
Originally Posted by g4aaw pete
As promised, measured on Fluke 87
a/c input = 244v a/c a/c o/p from transformer from ' 0' terminal to ' 250 ' terminal = 271v a/c Chassis to rectifier side of choke = 262v d.c. Other side of choke = 249v d.c.
Hope that's useful.
Regards Pete
Cheers Pete,
My measurements for transformer using AVO8:
i/p: 244VAC
o/p: 266VAC
6.3V 3A winding: 6.6VAC
Chassis to rectifier side of choke: 300VDC
Other side of choke: 283VDC
So, my output to the rectifier is actually lower than yours Pete, yet the final DC HT is considerably higher. What on earth is happening? Jim
I've just had a thought: there's another 40uF capacitor wired across the original by a previous owner. I've assumed this is because the original is duff but what would happen if it wasn't? I would then have the equivalent of an 80uF smoothing capacitor - would this cause a rise in HT voltage?
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
Hi Gerry , on another subject , regarding the AFseries of transistors does Tor say that the biasing resistors need changing to different values if AF types are fitted in lieu ?
Yes, there is still that original issue and as I think Roy noted, most likely a component problem on the circuits supplied by the stabilizer (have you tried changing the stabilizer by the way? – perhaps it is faulty).
Gerry
From:eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim Jobe Sent: June-16-12 8:44 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query
Hi Gerry,
I take on board all you've said. That's a useful tip on how to simulate a low impedance meter and I'll try that for comparison purposes. I've been using a DMM and also an AVO8 (see above for latest measurements as compared with another chap's set). When all's said and done though there is still that high current (47mA) through R66, measured with a series milliammeter, which is what alerted me in the first place and probably caused the original R66 to burn out, as well as, possibly, C115. I'll keep everyone in touch with what develops,
best wishes,
Jim
Quote:
Originally Posted by g4aaw pete
As promised, measured on Fluke 87
a/c input = 244v a/c a/c o/p from transformer from ' 0' terminal to ' 250 ' terminal = 271v a/c Chassis to rectifier side of choke = 262v d.c. Other side of choke = 249v d.c.
Hope that's useful.
Regards Pete
Cheers Pete,
My measurements for transformer using AVO8:
i/p: 244VAC
o/p: 266VAC
6.3V 3A winding: 6.6VAC
Chassis to rectifier side of choke: 300VDC
Other side of choke: 283VDC
So, my output to the rectifier is actually lower than yours Pete, yet the final DC HT is considerably higher. What on earth is happening? Jim
I've just had a thought: there's another 40uF capacitor wired across the original by a previous owner. I've assumed this is because the original is duff but what would happen if it wasn't? I would then have the equivalent of an 80uF smoothing capacitor - would this cause a rise in HT voltage?
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
Hi Jim,
I've with interest read about your problems with your 680X. You say that the
current through R66 is 47mA, I assume that the voltage at point F- is 150Volts.
The VR150/30 supplies three valves, the current taken in the BFO equals 6-7mA,
in the oscillator 4-5mA and the frequency changer about 12mA - all together
about 23mA. The regulator valve can take a maximum of 40mA, so that the current
in R66 might have been maximum 63mA, much lower than your 47mA. However 47mA in
2.7kOhms is 127Volts, add 150Volts from the regulator and your HT+ equals
277Volts - this is much above the value given in the handbook, 225Volts.
You mention that the input voltage is 244Volts AC, this is 6% higher than the
set needs. This means that the voltage at E- also is higher by 6%, perhaps
260Volts AC. If the 'Standby' switch is off then the receiver draws no current
and the capacitors C114 and C115 gets the full peak voltage - more than
360Volts, which is too much for C115.
I suggest you put a resistor in series with your AC-input to reduce the input
voltage to 230Volts AC or a little below - 100-200Ohms ought to do the trick.
Then when your input voltage is correct you can measure all the voltage points
in the diagram to find where your real problems are!
Good luck! Tor
Many thanks Tor. I actually measured the current through R66 by detaching one of its leads and inserting a millivoltmeter in series. I'll put a resistor in series with the supply as you say - I have a selection of different light bulbs which I'll try first but I wish I still had the Variac or one of the large rheostats I used to use when teaching!
Best wishes,
Jim
From: tor_marthinsen <tor_marthinsen@...> To: eddystone_radio_users@... Sent: Saturday, 16 June 2012, 19:37 Subject: [eddystone_radio_users] Voltages in a 680X
Hi Jim,
I've with interest read about your problems with your 680X. You say that the current through R66 is 47mA, I assume that the voltage at point F- is 150Volts. The VR150/30 supplies three valves, the current taken in the BFO equals 6-7mA, in the oscillator 4-5mA and the frequency changer about 12mA - all together about 23mA. The regulator valve can take a maximum of 40mA, so that the current in R66 might have been maximum 63mA, much lower than your 47mA. However 47mA in 2.7kOhms is 127Volts, add 150Volts from the regulator and your HT+ equals 277Volts - this is much above the value given in the handbook, 225Volts.
You mention that the input voltage is 244Volts AC, this is 6% higher than the set needs. This means that the voltage at E- also is higher by 6%, perhaps 260Volts AC. If the 'Standby' switch is off then the receiver draws no current and the capacitors C114 and C115 gets the full peak voltage - more than 360Volts, which is too much for C115.
I suggest you put a resistor in series with your AC-input to reduce the input voltage to 230Volts AC or a little below - 100-200Ohms ought to do the trick. Then when your input voltage is correct you can measure all the voltage points in the diagram to find where your real problems are!
Good luck! Tor
First thing I did Gerry and I also pulled the Oscillator, BFO and Mixer valves with no change in current drawn. The Stabiliser anode is at 151V so the excess current (measured directly) is caused purely by the enhanced HT Voltage. I'll try changing the rectifier as well tomorrow and completely replace the reservoir and smoothing capacitors, not just rely on bridging them with new components. There's one thing about obscure faults; they sure are interesting and get the old grey cells working! When I get time I intend going right through the set, checking all the capacitors and resistors as well,
Many thanks for your interest,
Jim
From: Gerry O'Hara <gerryohara@...> To: eddystone_radio_users@... Sent: Saturday, 16 June 2012, 18:33 Subject: RE: [eddystone_radio_users] Re: 680X query
Hi Jim,
Yes, there is still that original issue and as I think Roy noted, most likely a component problem on the circuits supplied by the stabilizer (have you tried changing the stabilizer by the way? – perhaps it is faulty).
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim Jobe Sent: June-16-12 8:44 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query
Hi Gerry,
I take on board
all you've said. That's a useful tip on how to simulate a low impedance meter and I'll try that for comparison purposes. I've been using a DMM and also an AVO8 (see above for latest measurements as compared with another chap's set). When all's said and done though there is still that high current (47mA) through R66, measured with a series milliammeter, which is what alerted me in the first place and probably caused the original R66 to burn out, as well as, possibly, C115. I'll keep everyone in touch with what develops,
best wishes,
Jim
Quote:
Originally Posted by g4aaw pete
As promised, measured on Fluke 87
a/c input = 244v a/c a/c o/p from
transformer from ' 0' terminal to ' 250 ' terminal = 271v a/c Chassis to rectifier side of choke = 262v d.c. Other side of choke = 249v d.c.
Hope that's useful.
Regards Pete
Cheers Pete,
My measurements for transformer using AVO8:
i/p: 244VAC
o/p: 266VAC
6.3V 3A winding: 6.6VAC
Chassis to rectifier side of choke: 300VDC
Other side of choke: 283VDC
So, my output to the rectifier is actually lower than yours Pete, yet the final DC HT is considerably higher. What on earth is happening? Jim
I've just had a thought: there's another 40uF capacitor wired across the original by a previous owner. I've assumed this is because the original is duff but what would happen if it wasn't? I would then have the equivalent of an 80uF smoothing capacitor - would this cause a rise in HT voltage?
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower
o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this
could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
I've connected 2X22ohm and a 33ohm resistor temporarily in series with the mains input and got the voltages down more or less where they should
be. I've also fitted new reservoir and smoothing capacitors. However, listening to some music on MW the audio sounds pretty awful. I know it's
not a HiFi set but a push-pull amplifier as the output should sound better than this does. So, next task is to have a look at the output stage, although it might be more sensible to check all the coupling capacitors first.
Jim
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Jim McGowan Sent: June-16-12 11:30 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Re: 680X query

Hi Gerry , on another subject , regarding the AFseries of transistors does Tor say that the biasing resistors need changing to different values if AF types are fitted in lieu ?
Yes, there is still that original issue and as I think Roy noted, most likely a component problem on the circuits supplied by the stabilizer (have you tried changing the stabilizer by the way? – perhaps it is faulty).
I take on board all you've said. That's a useful tip on how to simulate a low impedance meter and I'll try that for comparison purposes. I've been using a DMM and also an AVO8 (see above for latest measurements as compared with another chap's set). When all's said and done though there is still that high current (47mA) through R66, measured with a series milliammeter, which is what alerted me in the first place and probably caused the original R66 to burn out, as well as, possibly, C115. I'll keep everyone in touch with what develops,
best wishes,
Jim
Quote:
Originally Posted by g4aaw pete
As promised, measured on Fluke 87
a/c input = 244v a/c a/c o/p from transformer from ' 0' terminal to ' 250 ' terminal = 271v a/c Chassis to rectifier side of choke = 262v d.c. Other side of choke = 249v d.c.
Hope that's useful.
Regards Pete
Cheers Pete,
My measurements for transformer using AVO8:
i/p: 244VAC
o/p: 266VAC
6.3V 3A winding: 6.6VAC
Chassis to rectifier side of choke: 300VDC
Other side of choke: 283VDC
So, my output to the rectifier is actually lower than yours Pete, yet the final DC HT is considerably higher. What on earth is happening? Jim
I've just had a thought: there's another 40uF capacitor wired across the original by a previous owner. I've assumed this is because the original is duff but what would happen if it wasn't? I would then have the equivalent of an 80uF smoothing capacitor - would this cause a rise in HT voltage?
I note that you are checking voltages with a DMM – as you imply in the discussion, these instruments (even the cheapest ones) have a high Ohms per volt (‘o.p.v’) – usually tens of mohms, similar to a valve voltmeter (VTVM). The voltage table in the 680X manual provides nodal voltages using typical moving coil multimeters used ‘in the day’ with much lower o.p.v.: a ‘Weston’ and ‘AVO’ (note that the model of ‘AVO’ quoted is not a Model 8, and has an even lower o.p.v. than the ‘Weston, which is noted as only 1000 o.p.v.). I note that you make reference to this effect when discussing voltages you measure in the 680X circuit and, implicitly, this is especially the case in higher-impedance circuits (and as such a DMM will often read voltages significantly higher than in the 680X voltage table). In order to check against the figures in the table, you can easily simulate a lower o.p.v. meter for DC voltage ranges by placing a suitable resistor in parallel with the test leads, eg. on a 250v meter range, use a 250kohm resistor to simulate a 1000 o.p.v. meter sensitivity. Also, when making voltage measurements make sure the control settings are as stated in the table preamble – shorting the aerial, and settings for the RF gain and AGC in particular.
Your mains voltage is 6% higher than the 230vAC of the primary winding on the transformer. This would translate to 260vAC on one half of the secondary HT winding. Also, note that there is a 5% tolerance on voltages provided in the table, so this could be as high as 257vAC and still be (just) within tolerance – very close to the 260v to be expected from your 244vAC mains voltage. Have you measured the AC voltage across the 5Z4G anodes (should be between 520vAC given your mains voltage (type of meter will not make much difference here). If this is much higher, say by 5%, there may be a problem with the transformer, though a higher secondary voltage would be very unusual – maybe a partially shorted primary could cause this effect, but I have never come across that.
I've already though of that Roy but I think it's the 275V that is causing the high current, but that seems to be within spec as Eddystone quote 260V +-5% in the handbook (using a 1000ohm/Volt meter, not that that would make a difference in this case)
I tried pulling the HF Osc (EF91) and Mixer/Osc (6BE6) valves and that caused no change in the PD across R66 which was 122V. Interestingly, with all valves inserted and BFO off, this PD varies between 122V quiescent and 138V with RF pot turned fully down. Some valve(s) presumably increase their Ia with increasing signal input.
I might try increasing R66 in value when I find my stock of wirewounds.
Greetings friends of the group.
Today is a happy day for me, found in Brazil S680x Eddystone in a reasonable
state of repair and working very well.
As I said before, a radio is very rare in Brazil and I'm happy to be able to
afford.
The only problem is that this is not the center of the dial and the dial lamps
do not exist, but it is easy to get them.
I will photograph and put on my blog if anyone wants to take a look to make a
visit and leave a comment and I'll be very grateful.
Thanks to friends Gerry O'Hara, Andrew Kersey and all others who tried to help
me find an Eddystone al in the UK.
I'm reading the matter of Mr. Gerry O'Hara on the restoration of a S680X a
museum and I am finding it very nice.
Have not given up the idea of buying a radio directly from the UK,
but because of the high cost of shipping will wait a little longer to get
another radio.
Thank you, and for those who want to take a quick glance at Eddystone S680x I
bought here in Brazil, follow the link below. 73 all.
http://www.py2lsb.blogspot.com.br/2012/06/eddystone-s680x.html
PY2LSB - Ricardo
Aparecida City - GG77JE -
Brasil.
Hello All
I have just joined and am seeking help, as I just just purchased a 1995/2
receiver. It has the failed bite test however I don't have a service manual. I
don't have a circuit either. Can someone point me in the right direction. BTW
the battery on the cpu board what is it? is it the same as the 1650. One other
thing on the brochure it mentioned a 1161 panoramic display, anyone seen one? I
gather these are as rare as hens teeth.
73's Lee
Racal used to sell the Eddystone 1161 panoramic adapter under their
brand as Racal RA-1766 which I have. Inside it is all labelled
Eddystone.
73 de Jean-Claude, HB3YDH
Am 25.06.2012 16:33, schrieb vk5abc:
Hello All
I have just joined and am seeking help, as I just just
purchased a 1995/2 receiver. It has the failed bite test
however I don't have a service manual. I don't have a
circuit either. Can someone point me in the right
direction. BTW the battery on the cpu board what is it? is
it the same as the 1650. One other thing on the brochure
it mentioned a 1161 panoramic display, anyone seen one? I
gather these are as rare as hens teeth.
Do you have a photo and do you have a manual for the Racal RA-1766.
73’s Lee VK5ABC
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of casy_ch@... Sent: Tuesday, 26 June 2012 12:19 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Newbie
Racal used to sell the Eddystone 1161 panoramic adapter under their brand as Racal RA-1766 which I have. Inside it is all labelled Eddystone.
73 de Jean-Claude, HB3YDH
Am 25.06.2012 16:33, schrieb vk5abc:
Hello All I have just joined and am seeking help, as I just just purchased a 1995/2 receiver. It has the failed bite test however I don't have a service manual. I don't have a circuit either. Can someone point me in the right direction. BTW the battery on the cpu board what is it? is it the same as the 1650. One other thing on the brochure it mentioned a 1161 panoramic display, anyone seen one? I gather these are as rare as hens teeth.
I noted that the EUG website has ‘by request’ against the 1995 model (‘operator’s manual’) – may be worth emailing Chris Pettitt to see what he may have access to (g0eyo@...).
73
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of casy_ch@... Sent: June-25-12 7:49 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Newbie
Racal used to sell the Eddystone 1161 panoramic adapter under their brand as Racal RA-1766 which I have. Inside it is all labelled Eddystone.
73 de Jean-Claude, HB3YDH
Am 25.06.2012 16:33, schrieb vk5abc:
Hello All I have just joined and am seeking help, as I just just purchased a 1995/2 receiver. It has the failed bite test however I don't have a service manual. I don't have a circuit either. Can someone point me in the right direction. BTW the battery on the cpu board what is it? is it the same as the 1650. One other thing on the brochure it mentioned a 1161 panoramic display, anyone seen one? I gather these are as rare as hens teeth.
I have already done that and he is on vacation but told me he does not have the service manual thanks.
73’s Lee.
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of Gerry O'Hara Sent: Tuesday, 26 June 2012 2:19 AM To: eddystone_radio_users@... Subject: RE: [eddystone_radio_users] Newbie
Lee,
I noted that the EUG website has ‘by request’ against the 1995 model (‘operator’s manual’) – may be worth emailing Chris Pettitt to see what he may have access to (g0eyo@...).
73
Gerry
From: eddystone_radio_users@... [mailto:eddystone_radio_users@...] On Behalf Of casy_ch@... Sent: June-25-12 7:49 AM To: eddystone_radio_users@... Subject: Re: [eddystone_radio_users] Newbie
Racal used to sell the Eddystone 1161 panoramic adapter under their brand as Racal RA-1766 which I have. Inside it is all labelled Eddystone.
73 de Jean-Claude, HB3YDH
Am 25.06.2012 16:33, schrieb vk5abc:
Hello All I have just joined and am seeking help, as I just just purchased a 1995/2 receiver. It has the failed bite test however I don't have a service manual. I don't have a circuit either. Can someone point me in the right direction. BTW the battery on the cpu board what is it? is it the same as the 1650. One other thing on the brochure it mentioned a 1161 panoramic display, anyone seen one? I gather these are as rare as hens teeth.
Ian Nutt is considering getting some EC10 frequency scales made and needs to
judge what sort of demand there might be so is looking for expressions of
interest from EUGers. Ian thinks the cost would be in the region of £8-£15.
Please e mail Ian at iandcnutt@... if you would be interested
73s
Chris G0EYO
EUG Webmaster